So the saga begins. I didn't take pics a long the way, I never expected it to get this involved. It started as a simple enough tweak...
To fix the uneven shoulder, I used diamond files and stones to square the shoulder. Doing so caused my next set of woes, the tumbler face was also milled inline with the old shoulder, I now had high point that dug into the plate. So again more filing. I'm sure you guys who have worked on locks before realize at this point what a mess I'm and and my problems have only just begun. I'm a novice and had no idea what I was in for.
So, I had my shoulder squared, the face of the tumbler was now parallel to the lock plate, my spindle is sticking out at 90°. I reassemble for a test fit and find that the tumbler cannot rotate. Of course the side of the tumbler facing the bridle also now has a high point, and needs to be filed down so it doesn't impinge on the bridle. I finally get all that done (so I think) and have many hours into this already. I reassemble and after some testing, quite proud of myself, fire it several times then out of nowhere it gets stuck at half cock on the way down.
Queue ominous music...
I had reduced the thickness of the tumbler, leaving a gap big enough for the fly to fall out. At this point I'm panicking that I should have just sent it back. Why did I do this? Would they even take it back now?
After a a few deep breaths, I realize I can find the fly with a strong magnet and persevere. I very carefully filed down the boss to leave just enough clearance, and ensure it mounts the bridle parallel to the lock plate. Again I reassemble, only to find it still cannot rotate. After much measuring, blueprinting with a sharpie, head scratching, I finally realized the axis of the spindle has been moved to be 90° with the plate, the bridle is now closer to the plate and the hole is now misaligned. Tightening the bridle causes the tumbler to twist. After debating several possible fixes, I chose heresy, the ultimate bubba move, I enlarged the 2 mounting holes for the bridle so it could be rotated. I feel like a hack, but my welding skills are lacking. If I had confidence I could fill them without voids and without warping the bridle I would. I rationalize that between the 2 mounting holes, the screw for the sear, which serves as a 3rd mounting hole, and the tumbler pin and tight tolerances for the tumbler, I don't believe the mainspring could pull it out of position. This is an acceptable, if not ideal workaround in my opinion.
After finishing all of that I reassembled the lock and was quite pleased to find it functioned. I was also too burnt out from my emotional roller coaster and probably 20 hours fumbling my way through it.
So at this point I reinstalled it in the gun, and went shooting several times. And it worked, better than the old TC lock to boot. At this point I'm quite proud of myself. Next post I'll talk about polishing.