I wanted to report back because I appreciate those here who took their time to provide answers to my question. Today being yet ANOTHER rainy day in Berks County PA, I decided to dig into this project.
While I really appreciate Jim Kibler's very kind offer to do this for me, I wanted to try it myself. Knowing that I could buy interchangable replacement parts if I messed-up gave me confidence. Bottom line - it was easy-peasy to do, didn't take much time; and I ended-up with a crisp, slightly sub-2 pound trigger pull with zero creep or overtravel. Bashing things around a good bit to try jar the sear out of engagement with the cock at full bend, had no effect, so I feel the work did not compromise safely at all.
First, I carefully stoned the sear notch and the sear nose - not changing any angles, basically just mirror polishing with a very fine stone under magnification.
Then, I thinned the sear spring. I didn't want to use even a small grinder, like a Dremel, for fear to going too far, too fast with that already rather thin metal; and/or introducing any heat and screwing-up the temper. So, I just used a fine file and my engraving vise. I went very carefully, frequently going through the tedious process of reassembling the lock to test the strength of the spring. I filed the flat and a slight bevel on each side.

Eventually, I got it thin enough for the pull weight I wanted; then finished and polished the spring, so that hopefully no cracks could develop along the file stroke marks. This is the best pic I could get of the completed file work to try to show the final thickness of the spring. It's not a very good photo - sorry.

I didn't need to do anything to the mainspring.
All back together with a perfect rigger pull. Thanks again to those who helped and to Jim Kibler.

Greg